Work on getting the bad robots working
|Assignee:||Alex Zirbel||% Done:|
|Category:||Hardware||Estimated time:||5.00 hours|
Learn how to debug the robots with analog.
- % Done changed from 0 to 20
Fixed the bad wheel on bot 10 and took off the wires on the top. Hooray!
- Priority changed from Normal to High
Separate issue for different %Done statuses.
- Status changed from Assigned to Invalid
Interest in this should be directed to the new ticket for finding a day for Fleet Maintenance.
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